Friday, April 24, 2015

Arm Conclusion

4/24/15

My partners and I decided to focus on finishing and further improving the arm. We built our first model or rough draft at the beginning of the week and later ran various tests with it. When we discovered the issues, such as the speed of the arm, the endo-factors ability to pick up the tetrahedrons, and figuring out how to counter balance the entire square-bot so it wouldn't tip over, we  knew we would have to recreate the arm entirely. We have now finished what we think is our final design today, after various sets of testing we will begin to focus once again on the autonomous portion of the challenge.

No comments:

Post a Comment